On Monday, May 11th, we had a surge of power through our house so great, that it magnified the brightness of our lightbulbs tenfold.  The lights and one of the circuits proceeded to burn out, and the surge fried anything that was plugged in—as a strong burst of magnetic energy would. Even a surge strip did not keep the cable box from being fried. This type of situation has never occurred in our home in over 50 years. The event occurred at a little after 13:00 pm CST, or 18:00 UTC. No source was found for the surge, only a fried wire, which had caused a burning smell in the home. Certainly a malfunctioning wire, more than like fried by the surge as well, would not cause a surge in power, but a reduction in it. Would the Zetas care to comment on whether we are now experiencing  EMPs from PX on a more frequent basis? If so, would it be recommended that all electronics not in use be disconnected from their power source? Space was relatively quiet, but the magnetosphere was fluctuating widely. [and from another] http://www.manchestereveningnews.co.uk/news/greater-manchester-news... The cut was said to have been caused by an electrical surge. People in the area say "Smoke was coming from the electric cupboard from 86 Deansgate when the power surge hit. 4 fire engines responded to the call". Jade Barrow is a receptionist at 86 Deansgate, and said the whole building shook. She said: "The firemen explained to me that an electrical surge is like 2 magnets hitting each other. That's why it all shook because of the force."  [and from another]https://poleshift.ning.com/profiles/blog/show?id=3863141%3ABlogPost... May 15. After 15 days with approximately 300 hours of missing data, it appears the uninterrupted BATSRUS RCM image feed has resumed.


Air France 447 in 2009 and Malaysia 370 and the recent Germanwings A320 are in the news because they impact the airline industry, and the blame thus placed elsewhere. To date, pilot suicide, storms, and bad pilot judgement have been used, and how is the public to know otherwise? Electric trains such as the Disney Monorail  and DC Metro crash incidents in 2009 and the recent Amtrak 188 go into investigation while talking heads murmur about safety devices or track maintenance or mechanical failure, which ultimately get the blame.  

It is only when the public is broadly affected that the public can get a hint that something else is afoot. Cell phones are regularly having disrupted service but the blame is placed on blocked access to towers or bad weather. The blackberry outage in 2008 was blamed on a software glitch. If the public is frankly being lied to, engineers responsible for maintaining equipment and the grid are not fooled. The talk has spilled over into the press, or into conversations with the public. During the Washington DC blackout, the electrical problem was described at first by the Washington Post as a “surge”. 

This is a key determinant between a failed electrical system, a simple outage, and electro-magnetic pulse. Pulse is a surge, and the sudden increase in the amount of magnetons and their associated electrons, such that equipment controlled by a steady pace of either particle flow goes into a runaway state. When equipment is guarded by surge protection, to guard against lightning strikes, it will shut down, as a brownout situation can damage equipment. But unless a lightning strike was present, there can be no excuse for a pulse or surge other than the presence of the charged tail of Planet X, aka Nibiru.  

What can the public expect? As cell phone service and cable TV via satellite continues to degrade, as airplanes increasingly crash during complete electronics failure or are forced to land with smoke in their cockpits, as electric trains surge off the tracks and brakes fail, as transformers explode at dams and on the grid, and as residential lights flicker and erratic and unexplained and spotty blackouts descend, the public can expect endless inane excuses from the establishment. The truth will be withheld because mankind is so dependent upon his electrical systems and equipment that the thought of being without is unthinkable. It is mass denial. 

Source: ZetaTalk Chat Q&A for May 23, 2015

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Comment by jorge namour on January 23, 2017 at 2:09pm

United flights delayed after computer glitch grounds U.S. planes

http://www.reuters.com/article/us-ual-flights-idUSKBN15705C

A computer problem forced United Airlines (UAL.N) to ground all domestic flights for about an hour on Sunday evening, causing a cascade of delays and annoying customers throughout the United States.

The "ground halt", which the unit of United Continental Holdings Inc disclosed in a tweet at 8:06 pm ET and lifted about an hour later, follows a series of problems at United and other airlines last year.

International flights were not affected, the Federal Aviation Administration said. The number of flights that were affected was not known.

"The ground stop has been lifted. We're working to get flights on their way," United said in a tweet. bit.ly/2jQRW6B.

United said it would waive change fees for passengers with a 'travel waiver' but passengers took their frustration to social media and the Chicago-based airline started responding to their tweets.

"This has been the worst customer service experience and worst flying service ever experienced in 30+ years," one passenger tweeted.

"My minor son, the one stuck in Tampa with a tumor in his skull? You just told him he can't stay in a hotel. What's your plan?", another passenger tweeted to which the company responded asking for her son's travel details.

"We are working as quickly as possible to resolve this issue and get out customers to their final destinations," a company spokeswoman Maddie King said in an emailed statement earlier.

In October, thousands of United passengers were delayed worldwide after a computer glitch temporarily halted departures.

In June, software needed to dispatch United's flight plan briefly lost functionality and in July, the same airline's flights were disrupted after a computer problem blocked access to reservations records.

Last week, Air Canada (AC.TO) and Toronto-based Porter Airlines also experienced brief glitches that prompted some flight cancellations.

Comment by M. Difato on January 17, 2017 at 5:10pm

Amsterdam and the surrounding areas were plunged into darkness at 4.15 am local time leaving at least 364,000 customers without power and grinding the Dutch capital to a halt, according to reports. (Jan 17)

A state of emergency has been declared as a precaution.

As many as one million people could have been affected. Transportation services have been suspended and the mobile phone

network is reportedly down after being overloaded with calls.

The cause of the power outage was not immediately clear. The utility company Liander, said the fault originated at the

Hemweg power plant in Amsterdam. Just before 7 am, Liander reported that the number of affected customers had fallen to

199,000 after power was restored to 165,000 customers, many of them in the capital.

treet lights and traffic lights have been affected. Several websites hosted in Holland are down including the country’s largest

newspaper De Telegraaf. Police are asking people to refrain from calling except in case of emergency...."

Source: http://www.euronews.com/2017/01/17/amsterdam-blackout-leaves-364000...

Comment by M. Difato on January 11, 2017 at 10:15pm

 A Boeing 737 carrying the Dallas Stars National Hockey League team was forced to make an emergency landing after Smoke in cockpit (Jan 8) 

http://www.reuters.com/article/us-icehockey-nhl-dal-idUSKBN14S0XR

A plane carrying the Dallas Stars National Hockey League team was forced to make an emergency landing shortly after

takeoff at a St. Louis-area airport on Sunday because of smoke in the cockpit.

The Stars' Boeing 737 took off at 11:52 a.m. Central Time (5:52 PM GMT) from St. Louis Downtown Airport in Cahokia, Illinois.

But about five minutes later, the pilots turned the plane around and made the abrupt landing because of the smoke.

St. Louis Downtown Airport fire chief Mike Mavrogeorge told reporters that the smoke might have been caused by an electrical issue. He said there was not a fire.

The plane was carrying 50 passengers consisting of players, coaches and other team staff members.

The Stars confirmed the incident with a comment on their Twitter feed:

"After an emergency landing after takeoff due to an electrical issue, the team has boarded a new plane and is currently traveling to LA."

Comment by M. Difato on January 6, 2017 at 10:39pm

L.I.R.R. Train That Crashed (Jan 4) Was Going Over Twice Speed Limit, Inquiry Finds

http://www.nytimes.com/2017/01/05/nyregion/lirr-train-crash-speed-l...
A Long Island Rail Road train that crashed in Brooklyn on Wednesday was going more than twice the speed limit when it slammed into a train station, injuring more than 100 people, federal investigators said on Thursday.

The train was traveling at more than 10 miles per hour when it hit the end of the tracks at Atlantic Terminal, where the speed limit is 5 m.p.h., said Ted Turpin, an investigator for the National Transportation Safety Board. He said that federal officials were investigating the crash and had not yet determined the cause.

The train rammed into a bumping block during the morning rush, striking a room beyond the track and causing the first two cars to derail. The accident was reminiscent of a deadly crash in September in which a New Jersey Transit train plowed into Hoboken Terminal, killing a woman and injuring over 100 people. (That train was also traveling over twice the speed limit there when it crashed.)

On Thursday, Mr. Turpin said the engineer who was operating the Long Island Rail Road train told investigators he could not remember the crash.

“He does recall entering into the station and controlling the speed of the train,” Mr. Turpin said at a news conference. “But then the next thing he realized was after the collision.”

Investigators have not released the engineer’s name, but Mr. Turpin said that he was 50 and had started as an engineer at the railroad in 1999. The engineer had started working around midnight on Tuesday and was nearing the end of his shift at the time of the crash, Mr. Turpin said.

In the Hoboken crash, the engineer, Thomas Gallagher, also said he did not remember the crash. His lawyer later said that Mr. Gallagher had an undiagnosed sleep disorder and discovered after the crash that he had severe sleep apnea, which disrupts sleep and may cause excessive daytime sleepiness.

The engineer of the Long Island Rail Road train has been tested for drugs, but the results were not available, federal investigators said on Thursday. The engineer told investigators that he was not using his cellphone at the time of the crash.

Federal investigators said they planned on Friday to interview a conductor and an assistant conductor who were also on the train. They also intend to interview two railroad employees who witnessed the crash.

Mr. Turpin noted that a safety technology, known as positive train control, was not in place on the tracks where the crash happened, even though it was possible that the technology could have slowed the train. Officials from the safety board have long called for railroads to install the system to help prevent train accidents, though Mr. Turpin noted it was not required in train terminals.

Nearly two years ago, the Metropolitan Transportation Authority secured a nearly $1 billion loan from the Federal Railroad Administration to install positive train control on the Long Island Rail Road and Metro-North Railroad. Officials at the authority are working to meet a 2018 deadline to install the technology.

Comment by M. Difato on November 29, 2016 at 2:24pm

BOGOTA, Colombia -- A chartered plane with a Brazilian first division soccer team crashed near Medellin while on its way to the finals of a regional tournament, killing 76 people, Colombian officials said Tuesday. Only four people are believed to have survived.

The British Aerospace 146 short-haul plane, operated by a charter airline named LaMia, declared an emergency at 10 p.m. Monday (0300 GMT) because of an electrical failure, aviation authorities said. As CBSN’s Josh Elliot reports, the plane crashed not long after that, just five minutes from its destination.

The team, from southern Brazil and which had started its journey in Sao Paulo, was scheduled to play Wednesday in the first of a two-game Copa Sudamericana final against Atletico Nacional of Medellin.

“What was supposed to be a celebration has turned into a tragedy,” Medellin Mayor Federico Gutierrez said from the search and rescue command center..."

Source and full story: http://www.cbsnews.com/news/colombia-plane-crash-brazilian-chapecoe...

Comment by M. Difato on November 20, 2016 at 5:13pm

Qatar Airways flight from Miami makes emergency landing in Zurich (Nov 19)

http://gulfbusiness.com/qatar-airways-flight-from-miami-makes-emerg...

The flight’s crew reportedly detected smoke onboard the aircraft

A Qatar Airways flight travelling to Doha from Miami was forced to make an emergency landing in Zurich on Saturday

afternoon after crew detected smoke onboard.

Flight QR778 landed safely at the Zurich airport and requested emergency services to check whether there was any

problem.

All the passengers onboard the Boeing 777-300 were evacuated.

In a statement to Doha News, Qatar Airways said the flight was diverted because of a “technical issue.”

“Early indications point to a cooling fan malfunction. The aircraft landed safely. Safety and security are Qatar Airways’ highest

priorities,” it added.

A replacement Boeing 777-300 aircraft was dispatched from Doha to Zurich, and after picking up the passengers, returned to

the Qatari capital with an estimated total delay of 10 hours.

Comment by M. Difato on November 10, 2016 at 3:52pm

Horrific electrical explosions cause panic on UK commuter train (VIDEO)

https://www.rt.com/uk/366294-electrical-arc-train-dorset/

https://www.youtube.com/watch?v=V0XwgrSOmbo 

An electrical fault sparked an incredible series of explosions beneath a passenger train in Dorset, England.

Panicked passengers fled in terror as blinding explosions repeatedly erupted around them.Dramatic footage of the

Dorchester South Station incident captured bystanders yelling “get off the train” and “call an ambulance” in response to the

litany of loud bangs and 20ft-high (6 meters) sparks, reports the Metro.

The sparks were a result of ‘electrical arcing’ under the train, caused when electricity breaks down gas and creates on

ongoing discharge.

Despite the dramatic firework-like eruptions, no injuries were reported, according to a South West Trains spokesman.

Local rail services were delayed for two hours over the incident.

"Passengers were taken off the 18:03 Weymouth to Waterloo service at Dorchester South station after reports of

electrical arcing underneath the train.

"Emergency services were called as a precaution, but were not required. There was no fire, although the incident did

result in flashes, smoke and a bang, as well as cosmetic damage to the train."

Comment by M. Difato on November 10, 2016 at 3:07pm

Lack of braking results in the death of seven and more than 50 injured in London tram derailment (Nov 9)

 http://www.columbian.com/news/2016/nov/09/police-7-killed-in-london...

LONDON — Seven people were killed and more than 50 injured when a tram derailed while rounding a tight curve in a rainstorm in south London Wednesday, police said.

Investigators said the train, which tipped over on its side, apparently was going faster than permitted.

British Transport Police initially said five people had died, with several others seriously injured. The force later raised the death toll to seven.

Police arrested the 42-year-old tram driver on suspicion of manslaughter.

Emergency workers labored for hours to free five people trapped in the wreckage of the two-carriage tram tipped over next to an underpass.

The Rail Accident Investigation Branch said the tram derailed as it was negotiating a sharp curve with a speed limit of 12 mph.

“Initial indications suggest that the tram was traveling at a significantly higher speed than is permitted,” it said in a statement.

Passenger Martin Bamford, 30, said the train sped up and “everyone just literally went flying.”

“There was a woman that was on top of me … I don’t think she made it at all,” Bamford said outside Croydon University Hospital, where he was treated for rib injuries. “She wasn’t responsive. There was blood everywhere.”

Bamford said the driver told him that “he thinks he blacked out.”

Liam Lehane of the London Ambulance Service described many of the people hurt as “walking wounded” but said others suffered serious injuries.

London’s fire department said eight fire engines and four specialist rescue units were among the first responders to the Sandilands tram stop after the 6:10 a.m. accident.

“I heard a massive crash at about 6:15 a.m., then heard shouting, then the emergency services arrived,” said resident Hannah Collier, 23.

The British capital’s tram network serves 27 million passengers in the last year.

Wednesday’s derailment is the first tram accident with onboard fatalities since the 1950s, but official figures show that 20 people were injured in 112 tram-related accidents in the year to March, including one derailment and two collisions

Comment by Starr DiGiacomo on October 29, 2016 at 2:42am

http://fox61.com/2016/10/28/watch-fire-smoke-erupt-from-american-ai...

WATCH: Fire, smoke erupt from American Airlines plane after issue with takeoff at Chicago O’Hare

CHICAGO --A plane burst into flames at O'Hare International Airport in Chicago Friday afternoon during takeoff.

The American Airlines plane was taking off from Chicago at 2:35 p.m. CT en route to Miami when it blew a tire and had to abort the takeoff.

The 161 passengers and nine crew members on board were able to exit by sliding down a chute off the plane. They were then bused back to the terminal.

According to a statement from American Airlines, "Seven passengers and one flight attendant reported minor injuries and were transported to the hospital to be evaluated. We are taking care of our customers and crew and are re-accommodating our passengers on another flight to Miami this evening."

The blown tire caused a fire, and a huge column of smoke billowed above the plane.

The Federal Aviation Administration said in a tweet a runway was closed due to the disabled aircraft, and there was a ground stop for inbound flights.

The National Transportation Safety Board will investigate.

and then another:

http://fox6now.com/2016/10/28/fedex-plane-catches-fire-at-fort-laud...

PICTURES: FedEx plane catches fire at Fort Lauderdale airport

FORT LAUDERDALE, Fla. – A FedEx plane burst into flames Friday on a Fort Lauderdale runway, the same day that an American Airlines flight was evacuated in Chicago after catching fire.

A FedEx plane exploded in flames on a Fort Lauderdale, Florida runway Friday. (Courtesy: Kevan Shokat)

A FedEx plane exploded in flames on a Fort Lauderdale, Florida runway Friday. (Courtesy: Kevan Shokat)

The Federal Aviation Administration said that the landing gear of FedEx Flight 910 collapsed after it touched down, sending the DC-10 skidding along the runway before the aircraft caught fire. The plane was flying from Memphis, Tennessee.

Firefighters sprayed the plane with foam and extinguished the blaze.

The runway was shut down and delays are expected.

It wasn’t immediately clear if there were any injuries.

Comment by M. Difato on October 28, 2016 at 9:00pm

Flight from Philadelphia to Tampa diverts to Charlotte after crew smells smoke (Oct 27)

http://www.wbtv.com/story/33503084/flight-from-philadelphia-to-tamp...

A plane carrying passengers from Philadelphia to Tampa made an emergency landing in Charlotte Thursday evening.

The Southwest Air flight, number 3077, diverted to Charlotte out of "an abundance of caution," according to a spokesperson

for the company, after the crew smelled an odor similar to electrical smoke.

There is no word on what may have caused the odor.

The 737 plane was carrying 140 passengers and five crew members. Officials said an inbound flight would take the passengers

the rest of the way at 11:30 p.m.

http://www.wbtv.com/story/33503084/flight-from-philadelphia-to-tamp...

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